I rethinked the layout and decided that putting the pump on the supply side would save me a lot of work. It is the topology that the pump manufacturer recommends. I also reverted back to my earlier layout. With only six elbows I aimed to alignment the hot water supply down pipe to the corresponding manifold. That way when four more elbows arrives I only have to deal with aligning the cold return down pipe to the cold manifold. The supply side has the most ancillaries so I would make the most progressing.
To accomplish these I had to address routing the hot water supply pipes to accommodate the over-pressure valve, as well as the expansion tank which is daisy chained with the system feed. It was a tall order as I didn't plan and order those fittings. I had to rely on reusing old copper fittings from my scrap pile.
I reverted back to this original plan except changed the pump from the return to supply side; by putting the pump on the supply side I didn't need to move the manifolds outboard
the pump flange now is perfectly spaced from the back wall
a lot of soldering
The most difficult soldering were the joints at the heavy 1 1/4" brass valves as they have so much thermal mass. If your torch is under power you risk damaging the PTFE of the ball valve by burning it.
while dry fitting the most critical fittings I used masking tape to hold the fittings in place so I could carefully check the locations for the ancillaries, and the alignment of the supply down pipe (not yet install) to the plane of the supply manifold
once I finished checking I use this pipe to hold up the assembly and soldered the 10 joints in one go
one bad move could misalign all the fixings
the most difficult aspects of the plumbing is done; I even made the over-pressure discharge pipe
these few photos capture the intricate compound angles of the piping
the 1/2" port of the horizontal tee that shares with the over-pressure valve is for the expansion and system feeder
the expansion tank port is 5 1/2" from the wall
I was able to place the overpressure dischargee pipe close enough to the wall despite the test handle of the valve is angled in; I did this to reduce the plumbing complexity while accommodate the expansion tank connection that is 6.5" offset from the wall
With these done I wrapped up for the day. I re-compile the list of items that I need to procured:
1/2" 45 elbow, qty = 1
1/2" sweat ball valve, qty = 1
1 1/4" 90 elbow, qty = 4
Taco 1/25 hp IFC pump, qty = 1
hydronic thermostat with slab sensor, qty = 1
gallon size undiluted glycol, qty = 16
20A outlet with built-in switch, qty = 1
TBD supply hookup for the home made system feeder
I have a basic plan of the mount supports of plumbing. Most would be addressed with EMT conduit brackets with shim blocks. I might use Unistrut sparingly.
The diaphragm pump arrived. It is the lowest cost one powered by AC I found. I want one with low flow rate, low pressure, and with adjustable pressure switch. My goal is able to set it at 30 psi, but most of these pump are 50 PSI. They don't tell you how low the switch can be set to so the only way to find out is to buy one and test it.
I chose an AC powered so not to have a tacky 12Vdc adapter
not useful information other than there is a glimmer of hope to set it to 30 PSI
it is actually quite smooth and quiet; the problem of smartphone camera's audio AGC
with a $11 translucent fresh water jug from WinCo and some plumbing parts they will form the system feeder
I am designing out this $500 hydronic system feeder
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